b * “sm © taal — Ae 5 FIGURE 2—The tramline system at Cassiar. system from the normal drive. The high torque capab- ilities of this system have overcome start-up problems and the infinitely variable speed between 0 and 180 fpm (forward or reverse) has cut greasing time from 16 hours to 8. Loading The tramline loading is fully automatic (Fig. 3). Ore is transported from the crushing plant by conveyor and fed into a 100-ton-capacity bin. The bin is heated to prevent freezing of the ore, and kept empty to avoid freezing whenever the tramline is shut down. From the bin apron, feeders feed two counter-weighted air- operated 40-cu.-ft (1.12-m*) loading hoppers. The feeder is interlocked so that the apron feeder is shut off when the hopper reaches a pre-set weight. TABLE 2 — Financial Comparison of Delivery Systems Case 1 2 3 4 1,200,000 | 1,200,000 900,000 1,200,000 T. Line A | T. Line B (Riblet) | (Interstate) Unit Cost ($) 1.38 0.79 0.44 0.31 Cost per Year ($) 1,242,000 | 948,000 | 528,000 372,000 Savings per Year ($) 294,000 | 714,000 870,000 After-Tax Savings ($) 176,000 | 458,000 552,000 Capital Required ($) 3,223,000 | 3,973,000 | 4,313,000 Ratio — Capital Exp. to Income after Tax Rate of Yield — % Mine Rate Per Year Delivery Rate Per Year Method i 1,200,000 1,200,000 1,200,000 1,200,000 Present | Trucks *Costs in 1973 ($) RX ANOWSE os Siac Eth Sey As the car comes into the loading area, it passes an infra-red photo cell which activates a timer set to open the loader hopper as the car passes below. The control system allows loading to be done automatically from either one or both hoppers alternately or man- ually. A system of belts below the loading area removes any spillage. Cars The 142, 40-cu.-ft (1.12-m*) tramears are each mounted on two axles, with a two-wheel bogie at each end (Fig. 4). The initial wheels were a mixture of cast and fabricated units mounted on roller bearings. Below each truck are two brackets for attachment of the 214-in. open socket fitted to each end of the 214-ft (65.2-m) long, 214-in. (6x25 Langs lay) haulage rope. The socket is attached below the car with a steel pin through a bushing. The first modification made to the cars was the addition of a three-piece 14-in.-thick polyethylene lin- ing to help prevent the ore sticking during the altern- ately freezing and thawing weather conditions. This sticking has been further alleviated by installing a four-nozzle automatic blowpipe at the discharge ter- minal. The combination of these two have been effect- ive and have reduced spillage of ore from the cars. After only a short period of running, the pins hold- ing the haul-rope sockets to the cars were found to be spalling badly, preventing free movement of the socket. Several different designs of pin were used, but the only effective method of stopping the problem was to grease the pins at three-week intervals. Cassiar has recently modified a few tramcars and fitted bear- ings for the pin to rotate in; however, at this time we cannot say whether this will be successful. A third area of modification on the tramcars is the — 32 —