ected to the most obvious dust generating areas, such as con- veyors, transfer points and crusher discharges. This method was unsatisfactory as far as current emission standards are conterned, but did reduce dust levels inside the plant con- siderably and to less than 10 MPPCF average. Problems with duct plugging, fan blade overloading, and excessive maintenance were common, particularly in periods of cool weather. In the early 1970's studies were commenced to improve the dust control by engineered redesign of ductwork and enclosures, and some further improvement was achieved. With the introduction of proposed emission objectives for the mining industry and new asbestos air standards it became quite apparent that existing dust control systems would not be able to comply with the future requirements, and installation of new equipment was chosen as the desired course of action. It was also decided that at the same time a more effective inside dust control design would be instituted. We should note that as well as the current MPPCF TLV, asbestos operations also must meet a fiber per millilitre TLV, in effect a standard defining allowable fibre levels in the total dust concentration. The first stage of improvement was to install building insulation and a wall across the pan feeder bin and equip it with a flapped opening only at the base to allow ore passage to the jaw crusher. Prior to this a rubber flap had existed from the top of the building to the front of the pan feeder bin, and every time an ore truck backed up to discharge its load a con- centrated surge of displaced air and dust was pushed into the building interior, completely defeating exhaust hood systems. The new wall also tended to reduce heat loss to the outside.